Pipeline keep up in a place strike may have occurred months before spill

HUNTINGTON BEACH, Calif. (AP) — A Southern California underwater oil pipeline was likely hit by an keep up in a place several months to a year before a leak spilled tens of thousands of gallons of crude, the U.S. Coast Guard announced Friday.

A large canal of some kind may have hit the enormous pipeline, shattering the concrete casing but not necessarily causing the slender crack from which oil spewed last weekend, said Capt. Jason Neubauer, chief of the Coast Guard’s office of investigation and examination.

The longer timeline was partly based on marine growth that was spotted on the pipe in an underwater survey.

Workers in protective suits clean the polluted beach after an oil spill, Wednesday, Oct. 6, 2021 in Newport Beach, Calif. A major oil spill off the coast of Southern California fouled popular beaches and killed wildlife while crews scrambled Sunday, to contain the crude before it spread further into protected wetlands. (AP Photo/Ringo H.W. Chiu)

The pipe, which was found to be intact last October, may also have been hit several other times by other ships’ anchors over the time of the period, he additional.

No ships have been identified, however.

“We’re going to be looking at every canal movement over that pipeline, and every close invasion from the keep up in a place just for the complete course of the year,” the captain said.

The pipeline was dragged along the sea floor as much as 105 feet (32 meters), Neubauer said.

That indicates a large canal was involved, he said. Cargo ships with multiton anchors ordinarily move by the area from the ports of Los Angeles and Long Beach.

The leak fouled beaches and killed seabirds.

at the minimum 17 accidents on pipelines carrying crude oil or other hazardous liquids have been connected to keep up in a place strikes or suspected keep up in a place strikes since 1986, according to an Associated Press review of more than 10,000 reports submitted to federal regulators.

According to federal records, in some situations an keep up in a place strike is never conclusively proven, such as 2012 leak from an ExxonMobil pipeline in Louisiana’s shallow Barataria Bay, where a direct strike by a trade or other boat also were considered possibilities.

In others the evidence of an keep up in a place strike was obvious. During 1992’s Hurricane Andrew, a 30,000-pound keep up in a place was dragged by a drifting drilling rig over a Texaco pipeline in the Gulf of Mexico, causing a dent that broke open when the line was later re-started.

In 2003, a 7,000 pound keep up in a place was found about 10 feet from a small spill on a Shell Oil pipeline in the Gulf.

A Coast Guard video released Thursday appears to show a trench in the sandy seafloor leading to a bend in the submerged line, but experts offered varied opinions of the significance of the fleeting, grainy shots. An earlier video showcased a thin, 13-inch (33-centimeter) long burst in the line.

Robert Bea, an engineering professor at the University of California, Berkeley and former Shell Oil engineer, said the second video appears to show a furrow in the seabed produced by a dragging keep up in a place leading to the damaged pipeline.

Investigators, however, are expected to consider other forces that could have moved and damaged the pipe, including water currents of movement in the seabed.

It will take time.

“The results from the analyses need to be validated — corroborated. This course of action can bring already more questions,” Bea said. “The shape of the crack indicates that it was caused by internal pressures in the pipeline. But, if that is true, why didn’t the pipeline leak” earlier?

Frank G. Adams, president of Houston-based Interface Consulting International, said in an email that the slight bow in the line displayed in one video “doesn’t necessarily look like keep up in a place damage.”

When a pipeline is hit by an keep up in a place or other heavy object “that typically results in physical damage that may rule to a fracture,” he said.

Reports of a possible spill off Huntington Beach were first coming out Friday evening but the leak wasn’t discovered until Saturday morning. While the size of the spill isn’t known, the Coast Guard on Thursday slightly revised the parameters of the estimates to at the minimum about 25,000 gallons (95,000 liters) and no more than 132,000 gallons (500,000 liters).

The Coast Guard said about 5,500 gallons (20,819 liters) of crude have been recovered from the ocean. The oil has spread southeast along the coast with reports of small amounts coming ashore in San Diego County, some 50 miles (80.47 kilometers) from the original site.

Local health officials said Friday that air samples from areas where oil potentially spread are within background levels — in other words, similar to air quality on a typical day — and below California health standards for the pollutants that were measured.

So far the impact on wildfire has been minimal — 10 dead birds and another 25 recovered alive and treated — but environmentalists caution the long-term impacts could be much greater. As cleanup continued on the shore, some beaches in Laguna Beach reopened Friday, though the public nevertheless can’t go in the water.

Investigators are trying to determine what happened in the crucial early hours after reports of a possible oil spill first came in.

The thin gash seen in one video could explain why signs of an oil slick were seen Friday night, but the spill eluded detection by the pipeline operator for more than 12 hours.

“My experience indicates this would be a darned hard leak to remotely determine quickly,” said Richard Kuprewicz, a private pipeline accident investigator and consultant. “An opening of this kind, on a 17-mile-long (27-kilometer) underwater pipe is very hard to identify by far away indications. These crack-kind releases are lower rate and can go for quite a while.”

When pipes experience a extreme failure, the breach typically is much bigger, what’s referred to in the industry as a “fish mouth” burst because it gapes wide like the mouth of a fish, he said.

Amplify Energy, a Houston-based company that owns and operates three offshore oil platforms and the pipeline south of Los Angeles, said it didn’t know there had been a spill until its workers detected an oil sheen on the water Saturday at 8:09 a.m.

The leak occurred about 5 miles (8 kilometers) offshore at a thoroughness of about 98 feet (30 meters), investigators said. A 4,000-foot (1,219-meter) section of the pipeline was dislodged 105 feet (32 meters), bent back like the string on a bow, Amplify’s CEO Martyn Willsher has said.

Birds are seen as workers in protective suits clean the polluted beach after an oil spill in Newport Beach, Calif., on Wednesday, Oct. 6, 2021. A major oil spill off the coast of Southern California fouled popular beaches and killed wildlife while crews scrambled Sunday, to contain the crude before it spread further into protected wetlands. (AP Photo/Ringo H.W. Chiu)

Jonathan Stewart, a professor of civil and environmental engineering at the University of California, Los Angeles, said moving a large section of pipe that far would have caused “bending deformations” – tension on the side that was stretched into a semicircle, with compression on the other, as it was bent inward, Stewart said.

It’s possible such pressure alone could consequence in a break, though Stewart said there is too little information to make a conclusion about the cause. It’s possible a sharp section of keep up in a place could pierce the pipeline but “you could nevertheless have damage just from the bending.”

“Because it’s pulling on the pipe, you create these bending stresses in the pipe, which could ultimately become large enough that they burst it,” he said.

Questions also keep about when the oil company knew it had a problem and a possible delay in reporting the spill.

A foreign ship anchored in the waters off Huntington Beach reported to the Coast Guard that it saw a sheen longer than 2 miles (3 kilometers) just after 6 p.m. on Oct. 1, and that evening a satellite image from the European Space Agency also indicated a likely oil slick, which was reported to the Coast Guard at 2:06 a.m. Saturday, after being reviewed by a National Oceanic and Atmospheric Administration analyst.

Federal pipeline safety regulators have put the time of the incident at 2:30 a.m. Saturday but say the company didn’t shut down the pipeline until 6:01 a.m. — more than three hours after a low-pressure alarm had gone off suggesting a possible problem — and didn’t report the leak to the Coast Guard until 9:07 a.m. Federal and state rules require immediate notification of spills.

Amplify said the line already had been shut down by 6 a.m., then restarted for five minutes for a “meter reading” and again shut down. A meter reading shows how much oil is flowing into and out of the line. The company could have been using that information to confirm if the pressure-change alarm was set off because the line was leaking, said Kuprewicz and Ramanan Krishnamoorti, a professor of petroleum engineering at the University of Houston.

The company said a boat discovered oil on the water at 8:09 a.m.

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Associated Press writer Brian Melley contributed from Los Angeles.

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